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- zmotorsportsExplorerI have been needing to put new tires on our 2003 Monaco Dynasty. I have NOT been happy with the POS Goodyear G670 that were on the coach one bit. They have developed an irregular wear pattern and I thought I would have an alignment done prior to installing my new Michelin's.
The alignment was within spec but to the high side of the allowable thrust angle of the drive axle. Monaco Roadmaster rear suspensions are not adjustable, as many other heavy RV chassis are either. The guy who performed my laser alignment told me he wouldn't do anything with it as it was within the allowable range. That isn't me. Between he and I we calculated that the driver's side drive axle needed to move forward just under .125" and the tag axle slightly less than that.
On many heavy OTR trucks they use adjustable ends on their suspension links and Volvo uses an ecentric that allows for some slight adjustment. I thought about drilling the holes out and machining some ecentrics but wasn't sure if I wanted to lose any material on the chassis mounting points as well as several of them would be difficult to get a drill in due to space limitations.
Again, the gentleman who did the alignment suggested leaving it if there were no adverse handling issues. My wife and I like to travel mainly on two lane country roads when we travel and I notice that due to road crown the coach does drift off slightly when letting go of the steering wheel. On concrete interstates it is fine. I opted to move the driver's side forward .125" so it will actually help to hold to the road crown a bit.
First off, the reason for all this. Baby gets new shoes. Michelin XZA2 Energy tires in a 295/80R22.5 size. I am replacing all four drive tires, taking the two best tires from the drive axle and moving them to the tag axle and I will also be putting two new steer tires on. Good thing I am done paying for my son's college because there went a years tuition.:eyecrazy:

Here are the two trailing arms (control arms) that I will be removing to lengthen. Upper and lower on driver's side. Don't worry, all the weight of the coach is NOT sitting on those two jackstands under the hub. I have my 20-ton jackstands under the rear of the frame and those two 6-ton jackstands are merely holding the weight of the drive axle because I dumped the air out of the rear suspension to allow some movement of the axle.
Make-shift jig setup on my welding table. I clamped some large tubing down so I could make two borders to hold the trailing arm, take some measurements, cut and then insert the trailing arm back into the jig and clamp it to the correct length.
Cutting the trailing arm in my horizontal bandsaw.
I had measured the outside diameter of the square tubing of the trailing arms and had prepared for two separate methods of sleeving the trailing arm. I dug through my steel supply and found a piece of trailer hitch receiver tubing left over from one of the various trailer hitch projects. This measures 2" inside diameter and would work to sleeve the outside of the trailing arm. I was really hoping that the 2" square tubing that Roadmaster used for the trailing arms was .250" wall thickness because I also had a few small pieces of 1.5" O.D. x .250" wall square tube in my scrap bin. This would be my preferred method which would allow me to sleeve the trailing arm internally keeping the outside dimension the same as OEM. Not that sleeving it externally would be any weaker or stronger, just that I wanted to keep the trailing arm as near OEM appearance without sacrificing strength as possible.
All the planets were in alignment, the wall thickness of the trailing arm was .250" so I was able to use 1.5" square tubing to sleeve internally.:rocker:
I then went one step further and put the trailing arm back into the horizontal bandsaw and removed a .125" sliver of steel. This will allow me to have just enought of a gap in the joint to allow full penetration and let the weld bite hard into the inner sleeve as well as both halves of the trailing arm for a very solid link. In addition, I knew there would be some shrinkage or pull back putting that much heat and weld into the trailing arm. I actually set the overall length @ .156" thinking it would pull back approx. 1/32" upon cooling.
I also drilled a few .500" holes in both halves of the trailing arm to allow me to rosette weld (plug weld) the inner sleeve to the trailing arm. Root weld and rosette welds completed. For some reason I don't have any pictures of the internal sleeve but there is a 6" length of 1.5" square tubing inside the trailing arm.
While I was waiting for the root weld to cool slightly I decided to grab some polish and run a coat of polish around my wheels.
When my wife and I bought the coach in 2007 the previous owner had neglected the wheels badly. I don't think they had seen a coat of polish in their first four years. Upon our purchasing the coach, I removed all the wheels and polished them with a compounding pad using tripoli and jewelers rouge bringing them back to nearly new shine. Now once or twice a year I merely have to run around them with a coat of Busch's Aluminum polish and they look amazing and bead water off nicely.
I then moved on to complete to top pass on the trailing arm.
After cooling I threw it back into the jig to test for the final measurement. Dead nuts on @ 1/8" over the starting length. It shrunk back exactly where it needed to be.:rocker:
After cooling I applied a heavy coat of chassis paint, installed the lower trailing arm, removed the upper trailing arm and performed the exact same procedure. Here is the upper trailing arm completed and ready for paint.
Here is the upper trailing arm completed, painted and installed.
Here is the lower trailing arm completed, painted and installed.
Inner dual installed, Balance Master installed, Crossfire installed and torqueing the wheels on with my Proto 3/4" drive torque wrench. Yes that is snow that is starting to fall that you see on the ground. It started just as I crawled out from under the coach from tightening the last two bolts on the tag axle trailing arms.
View of completed project. You can see how much better it looks after all that work.:lol:

All in all, I am glad that job is done. Now to do another alignment just to confirm the modification.
Mike. - rollingslowExplorerResealed and cleaned the roof
- BEislerExplorerDrove past it sitting in storage and smiled, wishing for better weather when I can de-winterize and USE it! UGH!
- JumboJetExplorerTemperature was in the teens so I went and bought a 2nd Coleman Mach A/C to install. I just don't want it to get too warm.
- BigdogExplorerDecided that with 55 degrees and clear blue sky,that it was a good day to do a basement check on the MH. This turned out to be the first annual clean out and weigh day. Just kinda figgered that as long as I was pulling things out to clean the storage compartments that I'd see what I could get rid of and weigh the rest. Well, found that I had used almost everything at least once in the last 2 years and so it was a very small pile to get rid of.
I also found that the heaviest things,besides the DW's closet, were the tools (60#), the 14' folding ladder (27#),the slide with the chairs and mat (100#). Oh and the stock of liquid refreshments was close to 100#. The total weight for the basement was about 550# total
Also cleaned the windshield and side front windows. Used a mix of water and ammonia and that didn't do too much, so used a mix of windex and Rainex and that did better and that worked pretty good. Finally used Zep 505 and SOS pads and voila, none of those little white spots remained and no scratches on the glass. - JumboJetExplorerReplaced 15 year old CO detector with combination CO/LP detector.
Replaced 15 yer old LP detector with combination CO/LP detector.
Replaced 15 year old smoke detector with new one and added an additional smoke detector in the bedroom. - MrWizardModeratortoday..ran the portable generator
however on Feb 8, i replaced both the step motor and the step gear box with brand new replacement units - bigred1cavExplorerBest guess is cutout from when holes were made in tanks. Or grand kids.lol Mine put a tennis ball under sofa got caught when slide was moved, that was fun.
xctraveler wrote:
Okay, had a couple of hours in a campsite with no one close on my driver side. So it was time to tackle the stuck macerator.
I disconnected the hose from the pump and then had some fun flushing the connections and the ground nearby, fortunately there was not to much "stuff" in the hose (it broke while pumping black tank, but as the job was almost done). As soon as I flushed the pump entrance I could see a part of a white plastic disk jammed into the impeller. Reached in with my needle nose and extracted it. bump the switch and saw (and heard) the impeller spin. Put it all back together. Total time including cleanup 15 minutes. Extra time to clean me thoroughly but that was not part of the project.
Still wondering where that debris came from. The coach is almost 3 years old and we are full time so have been using the system regularly. I am hoping it was construction debris that just took its time finding its way to the exit. Can't imagine what it might have broken off of to get where it was. - McleoR0ExplorerRemoved about 30" of snow from my roof with accumulation that had occurred after 1/2 dozen or more of substantial snow storms covering a 2 month period I could not see my air condition cover. Went up on the roof did not stand because of ice packed due to thaw and refreeze However from my knees with a plastic shovel got it down to about a 1". I live in the Northeast and another storm coming this weekend I will sleep better tonight.
- xctravelerExplorerOkay, had a couple of hours in a campsite with no one close on my driver side. So it was time to tackle the stuck macerator.
I disconnected the hose from the pump and then had some fun flushing the connections and the ground nearby, fortunately there was not to much "stuff" in the hose (it broke while pumping black tank, but as the job was almost done). As soon as I flushed the pump entrance I could see a part of a white plastic disk jammed into the impeller. Reached in with my needle nose and extracted it. bump the switch and saw (and heard) the impeller spin. Put it all back together. Total time including cleanup 15 minutes. Extra time to clean me thoroughly but that was not part of the project.
Still wondering where that debris came from. The coach is almost 3 years old and we are full time so have been using the system regularly. I am hoping it was construction debris that just took its time finding its way to the exit. Can't imagine what it might have broken off of to get where it was.
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38,769 PostsLatest Activity: Dec 31, 2014